letterman7
06-19-2014, 04:43 PM
Hi folks,
Not a regular on the boards here, but ran into an interesting issue today. My PRT96 has been cutting relatively well for years (mainly, after Brady stopped by to help me tune it up a little), but it was never "just right". There was always just a touch of non-repeatability that bugs me - no two identically cut parts were exact. Very close, but maybe 1 or 2 mm off in one direction. Anyway, the past week I was cutting a file and one of the X motors hesitated and jumped a tooth or two. It happens - it's an older computer that gets buggy in certain weather, but usually both X motors will hesitate and screw up my cut (yes, I'm planning to upgrade very soon). Anyway, I reset and re-squared the Y carriage as close as I could get, measuring from the rail ends to the ends of the X rails, then following it up with a known good T square. All seemed good, and I continued on cutting my file.
Fast forward to today. I decided to surface my tabletop just because it was getting a little beat up. Today I just used my keyboard keypad to run the router via the user input rather than running a file to keep any errors out of the equation, so I ran the 2" end mill around the outside of the table first, then worked my was back and forth across the X axis. As I neared the far side of the table and had that strip of uncut material left, I thought it would be interesting to see how accurate it's actually cutting... and I was in for a rude surprise. The variation is about 1/8" across the length of the table - far too much for me (sample measurement shown):
21104
So the question comes into play: what do I need to tweak to get it to track straight? I thought it might be the motor that jumped and that the Y carriage isn't exactly perfect, so I unplugged and moved the carriage back by a tooth or two. I didn't want to go too far as I fear it might bind. Continuing the surfacing with the relocated pinion, it didn't seem to make any difference, so I took the strain back off that particular motor and re-squared the Y axis again. I'm a little stumped. I flunked geometry.. that's why I'm in the sign business!
Anyone have suggestions?
Thanks,
Rick
Not a regular on the boards here, but ran into an interesting issue today. My PRT96 has been cutting relatively well for years (mainly, after Brady stopped by to help me tune it up a little), but it was never "just right". There was always just a touch of non-repeatability that bugs me - no two identically cut parts were exact. Very close, but maybe 1 or 2 mm off in one direction. Anyway, the past week I was cutting a file and one of the X motors hesitated and jumped a tooth or two. It happens - it's an older computer that gets buggy in certain weather, but usually both X motors will hesitate and screw up my cut (yes, I'm planning to upgrade very soon). Anyway, I reset and re-squared the Y carriage as close as I could get, measuring from the rail ends to the ends of the X rails, then following it up with a known good T square. All seemed good, and I continued on cutting my file.
Fast forward to today. I decided to surface my tabletop just because it was getting a little beat up. Today I just used my keyboard keypad to run the router via the user input rather than running a file to keep any errors out of the equation, so I ran the 2" end mill around the outside of the table first, then worked my was back and forth across the X axis. As I neared the far side of the table and had that strip of uncut material left, I thought it would be interesting to see how accurate it's actually cutting... and I was in for a rude surprise. The variation is about 1/8" across the length of the table - far too much for me (sample measurement shown):
21104
So the question comes into play: what do I need to tweak to get it to track straight? I thought it might be the motor that jumped and that the Y carriage isn't exactly perfect, so I unplugged and moved the carriage back by a tooth or two. I didn't want to go too far as I fear it might bind. Continuing the surfacing with the relocated pinion, it didn't seem to make any difference, so I took the strain back off that particular motor and re-squared the Y axis again. I'm a little stumped. I flunked geometry.. that's why I'm in the sign business!
Anyone have suggestions?
Thanks,
Rick